Failure Analysis of Cracked P110 Repaired Tubing Used for Gas Transmission

天然气输送用P110裂纹修复油管失效分析

阅读:7
作者:Shuxin Zhang, Faqin Xie, Xiangqing Wu, Xi Yan, Jinheng Luo, Xiaoliang Ma, Gege Su

Abstract

With green and low-carbon developments in oil fields, an increasing amount of repaired oil tubing is being used as oil and gas transmission pipelines in China. However, due to differences in manufacturing standards between oil tubing and transmission pipelines, there are inevitably some issues during their use. This paper investigates a case of cracking failure in repaired oil tubing used as a gathering and transportation pipeline. The failure occurred after eight months of operation and was characterized by a circumferential crack at the male thread end of the tubing joint. To determine the root cause of the failure, a series of experiments were conducted on the oil tubing. The experiments included visual inspection, chemical composition analysis, mechanical properties testing, hardness testing, metallographic examination, and microstructure analysis. The results revealed that the thread of the cracked tubing was not tightened to the specified position; the connection between the tubing and the coupling was welded in a circumferential direction; and cracks occurred in the heat-affected zone of the weld. Chemical composition, tensile performance, and the Charpy impact of the tubing meet the requirements of API 5CT for P110 material, and no abnormalities were found in the metallographic structure. The microstructure at the weld toe of the fracture is martensite, and the hardness is 476 HV10. Based on the thermal simulation verification test, when the material of the tubing cools from 1200 °C, which is located in the coarse HAZ temperature zone, the base metal transforms into martensite with a little granular bainite, exhibiting its highest hardness value at 371 HV10, which is higher than the allowable hardness for carbon steel and indicates the material has poor weldability. The reasons for the cracking and failure of the tubing are that the P110 repaired tubing has a high carbon equivalent and poor weldability. During the welding process, martensitic structure was formed at the weld toe, and cold cracks appeared in the heat-affected zone, resulting in failure. To avoid the reoccurrence of such failure, recommendations are proposed.

特别声明

1、本页面内容包含部分的内容是基于公开信息的合理引用;引用内容仅为补充信息,不代表本站立场。

2、若认为本页面引用内容涉及侵权,请及时与本站联系,我们将第一时间处理。

3、其他媒体/个人如需使用本页面原创内容,需注明“来源:[生知库]”并获得授权;使用引用内容的,需自行联系原作者获得许可。

4、投稿及合作请联系:info@biocloudy.com。